October HL Contest Report – 10/21/17

October HL Contest Report – 10/21/17

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Hi fliers,
Today was a killer day for flying HL. The forecast blowout did not materialize this morning and did not ever get over about 8-10 with a few brief gusts to 15. Despite the persistent overcast, the lift was there and quite abundant. There were a couple of disappointments but nothing that cannot be repaired. If you weren’t there, you can kick yourself for missing a stellar opportunity to see some HL that was really KA.
Bill was very competitive in the early rounds and I kept finding myself saying, “why did I sell him my good planes?” He was leading through the first three rounds before a great round four put me in the lead to stay. Somewhere around round five Bill started having trouble finding the box and suffered a prolonged series of landouts that really took him out of contention.
Robert had his woes too. I think it was the last flight of round three that his Tweagle went in and broke the boom forcing him to go to his XXlite. Later on the XX went in as well and he had to fall back to a Stobel. ( I think his best rounds though came after the Stobel came out.)
I flew my new Vortex 3 for all rounds, though a couple of hard downwind dorks made me worry about breaking it. As the breeze came up in the middle rounds I put in a 13g ballast stick that settled things down a bit. Later I tried a 25g stick but that proved to be too much and I took it back out. (could have just been a couple of flights in strong sink but I blamed the ballast.) About the time I took it out the air improved and the last few rounds had some pretty fun flights. A shower came up and ran us off after round 11, but as soon as we had packed up, the rain ended, the wind died, and the sun came out. I’ll bet the lift in the afternoon was even better than this morning.
The full file is attached if you want to look at the play by play. I have pasted in the final results below.
It was a really fun day. I wish a lot more of you had come out to see it.
Wayne
btw, we have two more contests left this season; HL on Nov 4th, and Unl/2M on the 11th. See you there.
ps  some battery trivia for Robert. I turned my plane on at 9:15 this morning and did not turn it off until we finished. I estimate 3 hours of continuous on-time. My airborne recharge put back 245ma. put that in your pipe and smoke it…
Rank Name 1 2 3 4 5 6 7 8 9 10 11 12 Total Total W/Drops Drops Norm
1 Wayne 860 1000 1000 1000 1000 982 1000 524 1000 1000 1000 0 10366 8982 1384 1000.00
2 Robert 577 797 602 604 638 1000 958 1000 783 712 714 0 8385 7206 1179 802.27
3 Bill 1000 958 908 509 563 413 295 462 543 925 782 0 7358 6650 708 740.37

It was a great day for a contest.  I did well in the early going, as I’m used to sport flying in the lower winds we had in the first few rounds.  I didn’t do so well the later rounds after the wind picked up, but did not damage the Stream I was flying. Landing outside the boundaries to get a zero for at least 1 of the 3 flights in rounds 5 through 8 didn’t help at all.  Guess I need to practice in higher winds.
I flew the second Stream that Wayne sold me for the first time before the contest started, but chose to fly my other one in the contest that is 10 g heavier due to a few repaired dings.
I’ve attached a photo taken after the contest showing Wayne jubilant after his win and me with the sloper I brought along just in case the winds became REALLY strong.  (Actually I wanted to hand toss it, as I just brought it back to flying condition after buying it at one of the club auctions. It became the only plane I damaged today, as an attempt to throw it DLG style went bad as the wet wing slipped out of my hand.)
As to battery draw, my Stream was on for close to 3 hours during the contest and it took 178 mAhr to bring it back to full charge.  As it has a 700 mAhr battery, I could fly it all day long.  😎
Bill

Actually, I was fooled by the charger beeping when it reaches the point of decreasing the current from the 1C rate.  By the time the current got down to zero, I had 222 mAhr put back into the charger, so very similar to Wayne’s result.  Still safe for a lot of flying.
Bill

Hi Flyers:  Yes, my best rounds came after I went to the Stobel.  That is because it was the only plane I did not crash.

But the damage is minimal.  The Tweagle only broke the wing in several places, the fuse in several places and one servo gear.  The XXLite only broke the fuse in several places.

Mere flesh wounds.  It could have been worse.  Not much but ….

Darn!

Robert

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